Hello all. I'm new to the Orange tractor talks, but am not new to the workings of the L35 kubota GST.
I brought an L-35 into my shop for repair (would not move) . Found the Hydraulic clutch was broken, and metal and material were all over inside the case. Split tractor and replaced the manual clutch and the Hydraulic clutch and the Shuttle shaft, 2 shifters and pins. cleaned everything up and put tractor back together.
Fired it up and had no movement of tires. Got out the Pressure gauge and found GST has 350 psi to it. steering and hydraulics work. Check the Pilot circuit as in WSM page 3S51. no pressure at all. drained the oil again. used a blow nozzle on the hydraulic clutch to see if it locks up. it does, but I can still hear air leaking from what appears to be the mating surface of the hydraulic clutch to housing around the 2 oil rings. Is it ok if there is a little leakage of air when testing the clutch?
used compressed air to make the GST Valve operate. works like it should and moved shift shafts to proper location. have checked the modulate check valve, modulating valve, and pilot orifice for debris. appears to be correct. what else can I check to see If there is something else going on with the GST valve?
I brought an L-35 into my shop for repair (would not move) . Found the Hydraulic clutch was broken, and metal and material were all over inside the case. Split tractor and replaced the manual clutch and the Hydraulic clutch and the Shuttle shaft, 2 shifters and pins. cleaned everything up and put tractor back together.
Fired it up and had no movement of tires. Got out the Pressure gauge and found GST has 350 psi to it. steering and hydraulics work. Check the Pilot circuit as in WSM page 3S51. no pressure at all. drained the oil again. used a blow nozzle on the hydraulic clutch to see if it locks up. it does, but I can still hear air leaking from what appears to be the mating surface of the hydraulic clutch to housing around the 2 oil rings. Is it ok if there is a little leakage of air when testing the clutch?
used compressed air to make the GST Valve operate. works like it should and moved shift shafts to proper location. have checked the modulate check valve, modulating valve, and pilot orifice for debris. appears to be correct. what else can I check to see If there is something else going on with the GST valve?